‘Test, Don’t Guess’ When Lightning Strikes

It’s your best approach to tracking down the problem(s).

Problem description: Check electrical system. The battery goes dead after sitting a couple days.

“Oh, yeah,” the customer said, “there was a lightning strike in the parking lot where I work that might have affected the van.”

Most of the time, when I get in a vehicle that has a problem associated with a lightning strike, it’s due to an insurance company adjuster trying to determine the validity of the claim.

I have had the opportunity to deal with several actual lightning strike vehicles. Usually, various modules are fried. However, there was one that just threw me for a complete loop. That vehicle ran, but no electrical circuits in the body worked. Windows, door locks, radio, etc. I expected to find a main power circuit problem, but much to my dismay, there wasn’t a single blown fuse. The problem turned out to be on the ground side of this vehicle. The main body ground circuits that ran along the rocker panel under the driver-side doorsill were completely melted away.

This particular vehicle had only liability insurance, although the owner did say that four other vehicles in the parking lot had problems and all four were totaled by their insurance companies. “But,” he said, “they were closer to where it hit.” I informed my customer that if his vehicle did manage to become part of the lightning strike incident, that multiple modules may be involved and an accurate estimate would be difficult to obtain until after some investigation. The customer was fine with that and said to proceed step by step.

I started my drain tracing as I usually do by checking to make sure that none of the body input signals are active such as the door handle and closure switches. In other words, anything that would keep the body control awake. Getting a new body control module (BCM) for a bad switch input is a mistake I see made often in our line of work. Something as simple as having the key in the ignition will cause an input that keeps awake that body control module.

I like to wait an hour, when possible, before beginning a draw test with the vehicle properly at rest and have the hood open ahead of time. Next, I use a current probe attached – in this case – to my volt meter set on the Milliamp (mA) scale. The probe I use outputs a voltage signal that is directly proportionate to the current it sees when set on the low scale. This one was showing more than 700mA (Figure 1).

1014_TtT_Figure_1

Figure 1

This is well over the accepted at-rest current. In fact, for this model I typically see less than 30mA of at-rest current.

The next step is to find out where the excess current is going. I start this quest by eliminating one of the often overlooked but not uncommon causes: the alternator. By simply grasping the alternator’s feed and output circuits in the jaws of the probe, it is quickly eliminated as a suspect and I can move to the power distribution box (PDC) feed. This PDC has a quick release that allows me to lift it up from the battery box and have full access to its feed and output circuits. I measure the full current draw on the main feed (Figure 2).

1014_TtT_Figure_2

Figure 2

I can now measure the voltage drop across each of the PDC’s fuses to see which circuits are carrying current. So far I haven’t had to break any circuits to do my testing and risk waking any modules. By using the voltmeter’s millivolt (mV) scale I am getting a reading on two fuses.

Next, I go back to the current probe and read the current on the circuits under the fuse box leaving those two fuses and see that one of them is carrying most of the current. By using the wiring diagram, I am able to see that it’s the body control module carrying the current. With no discernible inputs, I make the determination that the module is the culprit. Before replacing the module, I print out the connector views and pin check each circuit to make sure I haven’t overlooked any circuits that I couldn’t parameter check.

“Test, Don’t Guess” has always been my motto. I like to think I have done all I can before replacing a nonreturnable module. I hate finding myself in the unenviable position of explaining to the customer the next “other necessary thing” that has to be done to fix the vehicle. I realize that sometimes it takes fixing one problem before finding another, but I’m not a big believer in the “chain reaction” theory that some use to explain all the parts they needed to replace to fix one problem.

The new BCM took care of the drain issue. I’m now getting 27 mA of “at-rest” current. I took the vehicle down the road for a test drive and discovered that the transmission was running in limp mode and the shift indicator lights were now boxed and blinking. The scan tool showed no data coming from the transmission control module.

Now the question becomes: “How many more modules are going to be a problem and how do I get to a bottom line estimate?”

The best way to proceed from here, in my opinion, is to make the customer aware of the possibility that there may be other modules involved and I need basically an open-ended authorization to continue.

After getting more time authorized to do further testing, I printed out the wiring diagram for the transmission control module (TCM) and the connector view.

The TCM is showing a P 1684 code, which just says the TCM has been disconnected. I figured I set that when I removed the connector to get the pin cover off. I did the power and ground test and got 12 volts on the battery circuit and good grounds.

Next, I checked the trans solenoid control circuits and couldn’t get any voltage on any of the solenoid circuits. I tested the transmission controls relay control circuit and couldn’t get any voltage there either. After back-tracing the control circuit, I discovered that the integrated power module (IPM) had an open in the circuit between the trans relay control circuit and the circuit from the transmission control module.

Since the PRND31 indicator was showing boxes around the letters, I went on measuring the voltages and comparing them to the diagram in the diagnostic chart. The numbers didn’t agree with the chart and the data voltage seemed odd with three of the four data switch circuits at 3.5 and the fourth one reading 7.4 volts.

The vehicle still started but ran with the transmission in limp mode. The park neutral start switch is separate from the PRNDL switch. This makes three more components that look to be possible victims of the high voltage from the lightning strike.

The customer was very cooperative in giving the authorization for the repairs and was thankful that we were even willing to work on the problem. I found out later that the customer had been to several places and had difficulty getting anyone willing to diagnose a lightning strike-related problem.