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Shop Transforms '06 Dodge Charger into Hot Rod for Greater CallingPosted 8/11/2011By Brian Manley
As professional technicians, we may often feel the desire to give back - to use our expertise for the betterment of our community. Recently, our shop adopted a special project from our local sheriff's department: a newly retired-from-the-fleet 2006 Dodge Charger. The sheriff, who initiated this project, is a drag racer from way back, and he wanted us to "build" the car for our local one-fourth mile drag strip, Bandimere Speedway. Our speedway hosts a program called "Take it to the Track" - an initiative aimed at getting young drag racers off the street and onto a safer venue. The reward for racing at the track is a head-to-head drag race with a police car! The more we talked about this project, the more excited we became and dived right in. The sheriff wanted to be more competitive with his Charger so he could win more than one third of his races. The Charger - here in Metro Denver - ran the quarter mile in 15.9 seconds and averaged 88 mph with the stock 5.7 Liter Hemi engine, automatic transmission and 2.80 differential gears.
We accepted the project, and with a generous donation from the Fraternal Order of Police, the sheriff delivered: • A higher lift roller camshaft and new roller lifters.
Our 5.7 liter Hemi engine includes a unique feature - the multi-displacement system (MDS) that deactivates four of the eight cylinders when the throttle is closed or at steady speeds. This is accomplished through the use of dual mode lifters and four solenoids that reduce oil pressure from 16 psi to 3 psi to close the intake and exhaust valves on cylinders 1, 4, 6 and 7.
Once apart, the engine looked like it was in great condition, and we made the decision to not bother the crankshaft, bearings and pistons. We simply swapped the cam and lifters and replaced all of the gaskets. After checking the cylinder heads for flatness, we carefully resealed all covers and installed the new headers. We were getting excited at this point, and we tried to invest as much time as we could to expedite this process, especially when we have a perfectly good engine scattered all over two benches for two weeks!
At the other end of our hot-rod-in-progress, we removed and disassembled the differential. We could definitely see the influence that Daimler-Benz had on this vehicle while removing the flexible, rubber coupler at the flange. It is important to mark mating surfaces when removing this shaft to prevent imbalance issues. It is also required to measure rotating torque before disassembling so it can be replicated later. A frustrating issue that we ran into here is that a case spreader needs to be used to remove and replace the ring and pinion gears; we do not have one. As much as we wanted to set up this differential ourselves, there were too many factors that led us to ask our friend at Chrysler to assist us - a friend with the case spreader and assortment of select shims, etc. that makes the job less frustrating. I have to say we ended up with a nice drive pattern! So, after 10 weeks of part-time volunteer labor involving six technicians, we were ready to install the differential, new exhaust system, start the engine and take her for a spin. I could not wait for our hot rod to be running because I desperately wanted to play with the flash reprogrammer and "tweak" different variables in pursuit of optimal performance. At this point the track was set to open in two weeks! In our next installment, I will reveal how (or if) the car ran at Bandimere Speedway and special issues that evolved with the powertrain control system. See you next time with the track report!
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